24 Hours of LeMons Travel and Tech Inspection Days

Travel day started off well. Everyone was in good spirits, well prepared for our 9-ish hour journey. Things went well until just after Canyonville, Oregon deep in the mountains. 5 of the 8 bolts securing the axel to the hub sheered off and 3 of them backed all the way out. This caused the engine to over-rev and exploded one of our radiator hoses.

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Pre-First-Inspection Festiva The 2nd day also started well and degraded with bad news. I personally was a bit of a dick and slept in a bit, but the rest of the team went to the track to get “a good spot”. We spent the first half of the day getting ready for tech.

We finally headed over to tech at 1pm, only to fail for a transmission leak that made itself evident when the car was jacked up on the passenger side and because our front wing (Pike’s Peak style) was “too sturdy”. We begrudgingly took off our lip, made a trip to the hardware store for a bolt, cut the bolt down to size, and riveted on some ABS plastic to make an air dam. Then with 30 minutes to spare, we took it over to tech and passed.

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