Race Preparation Mostly Complete

Over the last two weeks I’ve swapped springs (600/500 from 500/400), put in new trailing arm bushings, put in a MSI Direct Steering Kit, installed a new intercooler, drove to Oregon to get a ProTune from Tim Bailey, grinded, sealed, rolled, and pulled my rear fenders, got new Hoosier A6′s mounted, and I just now I’m finished up putting on my Hoosier stickers. I haven’t even washed my car yet.

I’m taking off in a couple of hours, I might still take out the backseats and seat belts as well as my amp/sub from under the front seats.

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Mod Weekend

This weekend I installed (well, I helped, Robby is a tour de force in the garage) new forward and rear trailing arm bushings, a new front control arm inner bushing, and upgrade the spring rates front and rear +100 lbs (600 lbs Front, 500 lbs rear). Body roll is pretty much nonexistent now. The main goal of the springs was to keep the rear tires off of the fender (they are gouging the tires and have stripped some paint).

Also, now that we have a new iPhone mount for the car, I can record some stable video. Here’s video of my winning run from event #5.

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TSnoCone

I co-drove John’s Elise on Sunday. It was the second time I’d drove it (first time in the dry and first time on slicks). I didn’t fair too well in the AM in class. John, however, managed to pull out a 2nd place trophy (out of 7). I ended up in 5th. I did manage to pull out a quick run on my last run of the day (a 44.4), which would have been the fastest time of the day had I not hit the cone on the way out of the slalom. Overall, I think things are looking to be fun for this WWSCC season.

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Progress on the E30

Despite the E30′s current engine problems (significantly down on power), Robby and I decided to press forward designing and fabricating the roll cage. One of the struggles of working in Robby’s shop is that he lives so far from supply shops that if you make a mistake, it can cost you a whole day of travel. Well, after traveling half a day to Lakewood and back, buying the the only piece of 1.5″ x 0.12″ DOM they had, our first hoop turned out too narrow because of an input error into the bend calculation software we were using.

The next day we drove all the way to Centralia to get another piece (this time 24′ in length, so there was enough extra for a whole hoop). This time things went much better, even though the bend calculator gave us the wrong cut length. Here’s a quick video of the bend preparation and the final product, which we’ll mount up on thick plates and a box.

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Video From the Last 2 NWR-SCCA Events

Here’s the video from event #5:

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Decent day for me, left a bit on the table (4th out of 8).

Here’s the video from event #6:

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Not a very good day for me overall, but good enough for 4th out of 7.

2010 NWR-SCCA Event #4

Here is the video of all 4 of my runs from yesterday’s event. The video was taken with my iPhone 4 (so 720p is available). I’m going to get a shorter mount hopefully, so it will be more stable. But other than the shaking from the mount, I was very pleased with the footage.

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Fast forward to the last run if you want to see my fastest run.

24 Hours of LeMons Recap

So, the race is over, our final result was 79th place (out of 106). The result isn’t very impressive, I know. But, at the very least, we finished the race. Which is especially good when you consider all the mechanical woes we had.

While our team captain, Richie, was completing the team’s 3rd lap, he spun on fairly mild corner. We all headed over to the penalty box to see what our punishment was, we all berated Richie and helped him with the punishment. Just as we finished writing “It’s too early in the morning for this shit” 100 times on the car, Rich noticed there was oil all over the front-passenger-side wheel. We pulled the car back into the pits and realized we didn’t have much of a choice other than replacing the main seals and the oil pan gasket. Almost 5 hours worth of work, luckily one of the local auto part stores had a main seal. After the work was done, we were then worried mostly about people getting seat time at all (in case the car didn’t make it), we rotated out drivers after 3 laps. After that, we did some longer rotations (still short) and then let Richie finish out the day.

Day 2 started with me putting the front air-damn back on after Richie broke it on Saturday when he lowered it onto the jack. That lip didn’t even make it through the first session as Rich spun the car coming down turn 5. This broke the air dam off again and tore the passenger-side-front tire off the wheel bead. We brought the car into the pits and did a fairly quick tire change (I was impressed considering how out of place everything was). Rich finished his hour stint, then it was John’s turn.

John’s hour went by without issue; then it was my turn. I went for just over 30 minutes before I tried a new line at turn 5 and spun it. I came in for my black flag and accepted the punishment having a steel cutout of 2 rabbits mating welded to our roof. Because the penalty took so long, I sent Richie out to finish my stint and run his.

Richie came in at the end of his stint; we thought because it was just time up, but that wasn’t the case. We lost the alternator belt. We called all the parts stores; they were all closed. At a last ditch effort, we ran around to other teams and asked, success! After a few minutes of getting the belt on, we were back out on the track.

It was Rich’s turn again. Rich started turning really fast times, managing one lap of a team best of 2:40. At the end of Rich’s session, he was black flagged again, this time for not negotiating turn 11 successfully and having to drive on the other side of the tire barriers. He convinced the judges his first spin was because the tire blew, so his penalty was to write “If I didn’t point out loopholes, I wouldn’t have to write this shit” 100 times. This took a long time because it’s a long ass sentence.

Then it was John’s turn again. John came back in with 15 minutes left for his turn because he apparently passed on yellow flag (which we find hard to believe because we couldn’t pass anyone). Because that was our 3rd counted penalty, we got a cone of shame stuck to the car (signifying we had 0 black flags left before being kicked off) and an hour penalty (which they only made us stay 40ish minutes of).

With about an hour left, we put 5 gallons in and I finished out the day, taking the checkered flag for the team. I was just running consistent, safe 2:44′s to try and get our lap count up. But hey, we finished! Overall, it was quite an adventure, having to rebuild basically the whole bottom end of the engine was quite a task. Luckily John and Richie knew what they were doing, because I sure didn’t.

Below is the extended length video of what we captured. I might put together a short highlight video later, but don’t hold your breath, there weren’t many highlights. ;)

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24 Hours of LeMons Travel and Tech Inspection Days

Travel day started off well. Everyone was in good spirits, well prepared for our 9-ish hour journey. Things went well until just after Canyonville, Oregon deep in the mountains. 5 of the 8 bolts securing the axel to the hub sheered off and 3 of them backed all the way out. This caused the engine to over-rev and exploded one of our radiator hoses.

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Pre-First-Inspection Festiva The 2nd day also started well and degraded with bad news. I personally was a bit of a dick and slept in a bit, but the rest of the team went to the track to get “a good spot”. We spent the first half of the day getting ready for tech.

We finally headed over to tech at 1pm, only to fail for a transmission leak that made itself evident when the car was jacked up on the passenger side and because our front wing (Pike’s Peak style) was “too sturdy”. We begrudgingly took off our lip, made a trip to the hardware store for a bolt, cut the bolt down to size, and riveted on some ABS plastic to make an air dam. Then with 30 minutes to spare, we took it over to tech and passed.

Catch Up

It’s been a while since I’ve posted because I’ve been extremely busy. So, here is a quick summary of what has been going on with my racing.

  • I got 2nd (out of 4) at the very wet/rainy 2010 Understeer event, which was good enough for a trophy.
  • I got 1st (out of 4) at the dry 2010 Oversteer event.
  • I got 4th (out of 10) at NWR-SCCA Event #2, which was good for my first ever NWR-SCCA event trophy! It was a pretty sweet trophy too.
  • Finally, my 2nd 24 Hours of LeMons team and I are heading down to Williows, CA tomorrow for the race this weekend. Technical inspection is Friday and the race is Sat/Sun. We’ll be driving the super-pimp Grouppe Festiva.

    Yay for Practical Jokes

    My work buddy, Craig, recovered my friend Corey’s keys that he lost a year ago down our black-hole stair case at work; but we didn’t let him know we had the keys. So, over the past few weeks before we went to lunch (Corey usually drives us all), I would go out and mess with his car just a little and then watched as he slowly started to think he was crazy.

    One day, I moved it just slightly into the next spot, then before we got into it for lunch, we mocked his parking job. This prompted a response of “Hrmmm, I didn’t think I parked on the line.” Then one time I cranked his stereo up and moved his seat forward a few inches. It was super hard not to laugh as he was verbally confused about his new seating position.

    Finally, today, he was parked where I normally parked. We switched his car back to where he normally parks and put my car back where it’s supposed to go. We also moved his seat all the way forward. His reaction was too hilarious, preventing us from containing our laughter in response to his “I think someone has been driving my car!” and “I swear I didn’t park there”, so I decided to finally give him his keys back. Good fun though.